Well, I got a praise report for ya. This one is fixed and one for my memory banks. I removed both exhaust manifolds and the left one was warped enough to pop the rear bolt and leave the rest buried in the head. Used a left hand drill bit and got lucky and got the rest of the bolt out. Ended up putting two new manfolds on it along with gaskets and all new hardware including ebp tube.
Removed turbo and y-pipe and egr pipe. The gasket between the two pipes was completely split and the bellows for each pipe has some leaks going on. Replaced these units and disassembled turbo and checked unison ring and vanes. These were ok so I put it back together and reoriented the clamp so it looked better. Reassembled truck and warmed up and allowed to perform a vgt relearn. Drove with ids and got a whopping 25 pounds of boost out of this tired ol girl. I must say I was impressed.
While trying to figure this thing out, I removed the aftermarket oil filter to see if it was collapsed or something stupid. It looked ok so I put it back in. After all was said and done this morning and she was idling in my bay, coworker comes over to me at the parts counter and says "you got oil gushing out of the bottom of that truck". Although it was not bad enough in his mind to shut it off!
So I run over and shut er down. It seems the filter o-ring let go. Now I get to relift the truck and change the oil and convert it back to Motorcraft parts. Then I get to degrease the whole thing and wash my floor to boot.
Ahh I feel a weight has been lifted off my shoulders.